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Customer:
A major Chinese refinery
Location:
Fujian, China
Tower Name:
C3 distillation column
Tower Diameter:
3000mm
Problem:
The rise in price of propylene on the market
spurred the customer to increase the propylene production
from LPG. They wanted to increase the capacity by 50%
and reach 270,000 tons/year (LPG base).
History:
The gas fractionation installation was originally designed
for capacity up to 180,000 tons/year (LPG base) and
its upper limit was 200,000 tons/year which is the constraint
to increase the capacity.
Solution:
Zehua's proprietary ADV high efficiency valve tray was
used to replace the existing conventional valve trays
in both De- C3 column and C3 distillation column. ADV
valves with more vapor channels provide better vapor
dispersion in liquid, thereby causing higher mass
transfer efficiency than conventional trays. Innovated
tray deck joint design increases the percentage of open
area and vapor bubble uniformity. For C3 distillation
column 200 trays were designed as 15% open percent and
20% downcomer percent. Bubble promoters were added to
enhance tray performance. New feed pipes, reflux pipes
and reboiler vapor return pipes were also modified and
added.
Results: The capacity
of the installation has reached 300,000 tons/year (LPG
base), which is 10% more than the designed target and contract
guarantee. The customer will not increase its capacity
anymore because of restrictions from the heat
exchangers. C3 distillation column efficiency has significantly
increased with better propane purity at smaller reflux
ratio. The propylene recovery has increased from 90%
to 95%.
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